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• Three astronauts were burned to death on the launch pad (1967)
• General Electric (GE) and other companies were commissioned to develop safety programs.
• These were developed based on combinations of existing programs for risk managements, such as those used by the Air Force, and Department of Defense.
• a definitive example of failure management
• the mission objective was to land on the surface of the moon, and return.
• the mission had four major components,
1. The booster (a saturn V rocket) was used for the initial launch, and was discarded after use.
2. The lunar module (dubbed Aquarius) was to be used for descent and ascent from the lunar surface, and to be discarded after use.
3. The service module was to be used for the trip to and from the moon.
4. The command module was equipped with a heat shield, and would be the only module to return to earth.
• In basic terms the mission had to be aborted as a result of an oxygen tank rupture. The fact that the astronauts managed to return back safely is a tribute to the quality of design in the space program.
• The events are chronicled below,
- during a test the booster oxygen tank drains (causing fires in nearby automobiles, sparked by ignition systems)
- a helium tank on the lunar module is found to have excessive pressure a number of times
- oxygen tanks that supplied breathing air and fuel cells were not draining properly. This was overcome by turning on heat, and redraining the tanks. No action was taken because the performance was adequate. It is believed that a problem arose at this point where insulation on wires inside the tank was worn down because of overheating, and the slower drain of oxygen from the tank.
- one of the backup crew (Charles Duke) got german measles, and had exposed one of the crew (Thomas Mattingly). He was replaced by Jack Swigert as the command module pilot. This crew had not had any experience together in critical situations.
- The Saturn V rocket burn is cut off 2 minutes early, requiring additional fuel to be burned to reach earth orbit. Fuel level were now lower, but not critical.
- one of the oxygen tank pressure gauges had gone off the scale and ground control had requested several times that the oxygen be stirred by a small fan in the tank.
- there were also pressure problems in a lunar module helium tank, and a hydrogen tank.
- a warning light indicates low pressure in a hydrogen tank in the service module. Fans in the tanks were turned on to stir up the hydrogen.
- an arc between two wires starts a fire in an oxygen tank fueled by the insulators. The pressure in the oxygen tank builds, and warnings are not sounded because they are overridden by the hydrogen tank warning. The fire spreads through the service module bay.
- a bang is heard, crew assumes it is a noisy valve actuation, and that it might have been done as a practical joke.
- the pressure has built enough to blow out an outer panel on the service module bay.
- the master power alarm sounds as power on a master bus is lost. This was caused by damaged oxygen lines to the fuel cells. It turns out that 2 of the 3 were off line.
- hatch to lunar module is closed.
- Huston is informed of the problem.
- readings are scrambled, pressures and temperatures appeared erratic. Oxygen pressure in one tank was zero, and dropping in another.
- a cloud is observed outside the service module
- the venting of gases causes the craft to drift off course, the guidance system fails, and the craft begins to wobble, interrupting communications with the ground.
- Huston is still taken by surprise, assuming that four failures indicated could not be related, and almost impossible independently, and they began looking for instrumentation problems.
- a battery for reentry was connected to the power bus, but disconnected to reduce power drain.
- Huston suggests disconnecting the 3rd fuel cell to check to see if oxygen loss was caused by the fuel cell. This operation could not be reversed.
- the goal of landing on the moon is no longer assumed possible, but the lunar module is kept intact for its supply of water and oxygen.
- the reentry battery is recharged and the command module is shut down, as the astronauts move to the lunar module. This is done acknowledging that the effects of the cold on the electronics is not known, and may affect earth reentry.
- it was decided to continue the flight path, and use the moons gravity to get back (with no lunar landing) for a total flight time of 100 hours.
- the remainder of the trip was punctuated by,
- cold (minimal power for heating left temperatures about 10°C)
- fatigue (standing room only, or sleeping in the cold service module)
- hunger (the food was meant to be mixed with hot water)
- thirst (water was generated by the fuel cells)
- the CO2 was normally absorbed by filters. With the extra use the filters in the lunar module were exhausted. The filters from the service module were not the correct shape to fit, requiring a jury rigged arrangement using duct tape.
- a new reentry procedure was devised and had to be relayed verbally to the crew and written on paper (not plentiful). This checklist took 2 hours to transmit verbally.
- The astronauts moved back to the command module, powered up the equipment (luckily the effects of the cold did not cause any malfunctions). There was a new concern that the heat shield was still intact. No instruments allowed this to be checked. The other modules were jettisoned.
- the spacecraft landing began, and finished safely, with one of the fastest recoveries.
• In retrospect the accident was reviewed, and the causes for this accident were believed to be,
- budget pressures, morale problems, and schedule pressures encouraged the use of the damaged oxygen tank.
- the estimates of failure effects had been incomplete because of assumptions of adequacy.
- emergency plans were available but not practiced.
• The Challenger accident would have been prevented with the existing NASA procedures. The explosion of the Challenger is more the result of management failure in NASA and Morton Thiokol than the result of technical failures.
• In general the important notes are,
1972 - contract awarded to Morton Thiokol to design the Solid Rocket Boosters (SRBs)
- the design is based on a modified Titan III rocket, with significant design changes
- one of the changes was an o-ring seal along the rocket body. The joint was made longer, and a second ring added to provide a redundant seal.
1977-78 - An engineer discovers during tests that under pressure the joints rotated significantly causing the secondary o-ring to become ineffective. This is a result of the elongated joint to hold the secondary o-ring. Morton Thiokol management did not recognize the problem.
1980 - The joint is classified on the CIL (Critical Item List) as 1R, indicating that failure would be catastrophic, but there is a redundant o-ring to act as a backup in the event of failure. This was only one of 700 items listed as criticality 1.
1981 - the shuttle begins orbital testing
1982 - the space shuttle is declared operational
- After a few flights, problems with the o-rings were noted, as were other items. The normal procedure was to assign a problem tracking number, and examine the causes. This was not done for the o-ring problem. Eventually the problem was recognized and the rating was changed to 1 on the CIL. It was shown that despite NASA’s reclassification, the system was still listed as 1R in the Morton Thiokol paperwork, as well as a number of other documents. Also, Morton Thiokol disagreed with the criticality change, and went to a referee procedure.
1984 - the erosion of the o-rings has become a significant concern, and review procedures are requested for the packing of the o-ring joint with the asbestos filled putty that prevents heating of the rings. Morton Thiokol responds with a letter suggesting that higher pressures used in testing the joints was resulting in channels in the putty, and increased erosion of the o-rings. statistics from before and after the change in testing pressure seemed to confirm this. Morton Thiokol recommends continuing the tests to ensure sealing despite the problems, and begins investigating the effects of the testing on the putty.
Jan 1985 - A launch of a space shuttle at the coldest temperatures to date leads to the greatest failure of the o-rings to date. The o-rings will deform under pressure to seal the gap, but this is hindered when they are colder, and the material stiffer.
Jan-April 1985 - Continued flights and investigations show continued problems with the o-rings, and a relationship to launch temperature. Morton Thiokol acknowledges the problem, and the effects of temperature, but concludes that the second o-ring will ensure safety.
April 1985 - the primary o-ring does not seal, and the secondary ring carries the pressure, with some blowby (i.e., the backup was starting to fail). As a result a committee concludes that the shuttle must only be operated in an acceptable flight envelope for the o-ring seal. This report is received by Morton Thiokol, but does not seem to be properly distributed. The problem was also not properly reported within NASA to upper management.
July 1985 - A Morton Thiokol engineer recommends that a team be set up to study the o-ring seal problem, citing a potential disaster.
August 1985 - Morton Thiokol and NASA managers brief NASA headquarters on the o-ring problems, with a recommendation to continue flights, but step up investigations. A Morton Thiokol task force is set up.
October 1985 - The head of the Thiokol task force complains to management about lack of cooperation and support.
December 1985 - One Thiokol engineer suggests stopping shipments of SRBs until the problem is fixed. Thiokol writes a memo to NASA suggesting that the problem tracking of the o-rings be discontinued. This lead to an erroneous listing of the problem as closed, meaning that it would not be considered as critical during launch.
Jan 1986 - The space shuttle Challenger is prepared to launch Jan., 22, originally it was scheduled for July 1985, and postponed 3 times, and scrubbed once. It was rescheduled again to the 23rd, then 25th, then 27th, then 28th. This was a result of weather, equipment, scheduling, and other problems.
Jan., 27th, 1986 - The shuttle begins preparation for launch the next day, despite predicted temperatures below freezing (26°F) at launch time. Thiokol engineers express concerns over low temperatures, and suggests NASA managers be notified (this was not done). A minimum launch temperature of 53°F had been suggested to NASA. There was no technical opinion supporting the launch at this point. The NASA representative discussing the launch objected to Thiokol’s engineers opinions, and accused them of changing their opinions. Upper management became involved with the process, and “convinced” the technical staff to withdraw objections to the launch. Management at Thiokol gave the go ahead to launch under pressure from NASA officials (this was the critical decision).
- the shuttle is wheeled out to the launch pad. Rain has frozen on the launch pad, and may have gotten into the SRB joints and frozen there also.
Jan., 28th, 1986 - The shuttle director gives the OK to launch, without having been informed of the Thiokol concerns. The temperature is 36°F.
11:39 am - The engines are ignited, and a puff of black smoke can be seen blowing from the right SRB. As the shuttle rises the gas can be seen blowing by the o-rings. The vibrations experienced in the first 30 seconds of flight are the worst encountered to date.
11:40 am - A flame jet from the SRB starts to cut into the liquid fuel engine tank, and a support strut.
11:40:15 am - the strut gives way, and the SRB pointed nose cone pierces the liquid fuel tank. The resulting explosion totally destroys the shuttle and crew.
11:40:50 am - the SRB’s are destroyed by the range safety officer.